Can someone please assist me in reviewing my dbotcorexy.cfg against my Marlin Configuration.h files? I am building a D-Bot CoreXY printer and I was having issues with my Arduino/RAMPS setup in which my XY would randomly move diagonally. I felt this could be due to the CoreXY kinematics and cheap Arduino/RAMPS boards. I have purchased and configured/wired a BBB/Replicape setup but now I am having issues where the motors make noise, but do not move. My motors are 42BYGHW811P1 models.
Any assistance would be appreciated.
https://drive.google.com/file/d/0B3dl-8-2xS0gdXdtS0ZiZXJBeHM/view?usp=sharing