Can someone please assist me in reviewing my dbotcorexy.cfg against my Marlin Configuration.h files?

Can someone please assist me in reviewing my dbotcorexy.cfg against my Marlin Configuration.h files? I am building a D-Bot CoreXY printer and I was having issues with my Arduino/RAMPS setup in which my XY would randomly move diagonally. I felt this could be due to the CoreXY kinematics and cheap Arduino/RAMPS boards. I have purchased and configured/wired a BBB/Replicape setup but now I am having issues where the motors make noise, but do not move. My motors are 42BYGHW811P1 models.

Any assistance would be appreciated.

https://drive.google.com/file/d/0B3dl-8-2xS0gdXdtS0ZiZXJBeHM/view?usp=sharing

And here is my dbotcorexy.cfg file.

https://drive.google.com/file/d/0B3dl-8-2xS0gN0FVbkotOG41Wnc/view?usp=sharing

i try replicape for the first time yesterday whit slight modification to your config file and its work your issue is probably hardware

@Simon-Gabriel_Gervai what version of the Replicape are you using and what version of Kamikaze?

@Simon-Gabriel_Gervai can you verify the motor wiring as being Rev B3: 1, 2, 3, 4 = OA2, OA1, OB1, OB2 where pin 1 is the closest to the power terminals (furthest from the Ethernet port).

im using the revb3 whit kamikaze 2.0.8 i use this motor http://www.automationtechnologiesinc.com/products-page/3d-printer/nema17-stepper-motor-kl17h247-150-4a-for-3d-printer

wire order is :red green yellow blue from the power side.
hope its clear enough to help you

http://www.automationtechnologiesinc.com/products-page/3d-printer/nema17-stepper-motor-kl17h247-150-4a-for-3d-printer